潘集选煤厂智能化建设实践与探索

    Practice and exploration of intelligent construction in Panji Coal Preparation Plant

    • 摘要: 为解决洗选控制难度高、人工效率低、药剂用量与能耗偏高、产品质量不稳定等一系列问题,潘集选煤厂构建了覆盖洗选全流程的智能化体系,通过构建重介分选、浮选、煤泥分选等智能控制系统,创新管控工位替代固定岗位的管理模式,搭建数据湖体系、综合能耗管理子系统、设备远程诊断系统等智能管控体系,提升选煤厂智能化运行水平与生产综合效益;通过开展采制化对比试验、浮选加药对比试验与煤泥筛分试验,采用配对样本t检验的统计学方法对智能化建设成效进行定量验证与分析。结果表明:智能采制化系统单次检测耗时缩至30 min以内,检测效率较人工检测提升75%;浮选精煤合格率提升至95%,较人工加药提高15个百分点,起泡剂、捕收剂用量分别降低 4%与2%;> 0.125 mm粒级煤泥几乎全部回收。生产运营层面,岗位用工较设计定员降低52%,吨煤电耗从11.63 kW·h降至11.38 kW·h,吨煤介耗从 0.98 kg降至0.70 kg,万吨原煤事故影响时间由0.57 h缩短至0.43 h,干煤泥产品水分降至18%以下。潘集选煤厂形成了技术适配、人员转型、数据贯通、成本可控的智能化建设模式,所形成的工程实践经验可复制、可推广,为国内选煤行业智能化升级提供了参考与示范。

       

      Abstract: To address a series of challenges such as high control difficulty, low manual efficiency, excessive reagent and energy consumption, and unstable product quality, the Panji Coal Preparation Plant has constructed an intelligent system covering the entire washing and separation process. By building intelligent control systems for heavy medium separation, flotation, and coal slime separation, the plant innovated a management model that substitutes functional workstations for fixed positions. Furthermore, it established an intelligent management and control framework comprising a data lake system, a comprehensive energy consumption management subsystem, and an equipment remote diagnosis system, thereby enhancing intelligent operation levels and overall production benefits. The effectiveness of the intelligent construction was quantitatively verified and analyzed through comparative tests of “sampling, preparation, and assaying” flotation reagent dosage, and coal slime screening, utilizing the statistical method of paired-sample t-tests. The results indicate that the single detection time of the intelligent sampling, preparation, and assaying system was reduced to within 30 min, with detection efficiency increasing by 75% compared to manual methods. The qualification rate of flotation clean coal rose to 95% (a 15 percentage point increase over manual dosing), while the dosages of foaming agents and collectors decreased by 4% and 2%, respectively. Additionally, coal slime with a particle size of > 0.125 mm was almost entirely recovered. At the operational level, labor requirements were reduced by 52% compared to the designed staffing level. Power consumption per ton of coal decreased from 11.63 kW·h to 11.38 kW·h, and heavy medium consumption fell from 0.98 kg to 0.70 kg. The accident impact time per 10,000 tons of raw coal was shortened from 0.57 h to 0.43 h, and the moisture content of dry coal slime products was reduced to below 18%. Panji Coal Preparation Plant has successfully developed an intelligent construction model characterized by technical adaptation, personnel transformation, data integration, and cost control. The resulting engineering experience is replicable and scalable, providing a reference and demonstration for the intelligent upgrading of the domestic coal preparation industry.

       

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